Water Industry Process Automation & Control Monthly - April 2024
Record Well Drilled in Oklahoma
1. PROVEN RESULTS
Record well drilled in Kingfisher County, Oklahoma. Spud to
TD in 8.43 days, 1449 ft/day average.
Operator Location
Oklahoma Energy Acquisitions Kingfisher County, Oklahoma, USA
Well Type Total Runs
Horizontal 4 (Surface-Intermediate-Dedicated Curve-Lateral)
Distance Drilled Job Duration
12,215 ft 126.83 Drilling hours
Overall Average ROP Products/Services
93.07’/hr Aim-Contender Motors
RTOC Survey QA/QC & Distance Monitoring
(Contact an Aim rep. for more information)
Customer Objectives
• Drill from spud (Including Surface Hole) to total depth(TD) in 10.50 days.
• Minimize sliding and dog legs while maximizing ROP.
• Maintain tight target constraints for wellbore placement.
Results
• Drilled from spud (Includes Surface Hole) to total depth (TD) in 8.43 Days
• Stayed within the required geological target with minimal sliding (Slide – 10%, Rotate – 90%)
• Reduced overall NPT and drilled a highly efficient well
Value to Client
• Reduced days and cost on the well.
• The minimal sliding and reduced dog legs improved running casing.
• The operator experienced minimal NPT allowing the focus to stay on quality drilling and operations for the entire well.
Trinidad Pena
Director of Sales