Q2-3 well, the reason of decreasing oil production is that the high wax in crude oil near wellbore resulted in plugging after analysis.We carried out BERO treatment on Q2-3 well, mixed with formation water. The temperature of the injection fluid above 50 ℃.Pressure in the process of construction increased from 0 psi to 1450 psi. Q2-3 well was in close well to resume production in 5 days.Q2-3 shows base oil from 3.9 BOPD to 8.8 BOPD.