SlideShare une entreprise Scribd logo
Tune Case (NH)
Experience from Clean-up and
Production using formate based
brines as drilling/completion fluids
Drilling & Completion Fluid Seminar, Aberdeen 03.06.24
By Stine Bøhle Karlsen, Production Technology Tune
Agenda – 03.06.24
Tune Field Information
Initial clean-up / Normal Production Tune
3500
3500
3500
3500
3500
3500
35003500
3500
35003500
3500
3500
3500
3500
3500 3500
PPP
478000 479000 480000 481000
6701000
6702000
6703000
6704000
6705000
6706000
0 500 1000m
30/8-A-14H
30/8-A-12 H
30/8-A-13H/AH
30/8-3
30/8-1S
30/8-A-11
H
3750
3750
3750
3500
3500
3500
3500
35003500
3500
3500
3500
3500
3500
3500
PPP
475000 480000 485000
6695000
6700000
6705000
6710000
3850 - 3900
3800 - 3850
3750 - 3800
3700 - 3750
3650 - 3700
3600 - 3650
3550 - 3600
3500 - 3550
3450 - 3500
3400 - 3450
3350 - 3400
3300 - 3350
3250 - 3300
3200 - 3250
0 2000 4000m
30/8-A-12 H
30/8-A-13 H/AH
30/8-1S
30/8-A-11
H
30/8-A-14
H
Tune Field
 Horizontal gas producers
 Pure gas depletion
 Sand screen completion
 Tarbert Formation
 Gas/condensate
 HP/HT – 525 bar / 131 degC
 Reservoir thickness 100m - N/G 0.85
 porosity ~16%, permeability 10-200 mD
 12 m oil rim – non commercial
30/5-2
Agenda – 03.06.24
Tune Key data
Initial clean-up / Normal Production Tune
Initial clean-up Tune
PDO
 To drilling rig (Deep Sea Delta)
 2-3 weeks after final completion
Actual
 To Oseberg Field Centre (through 11 km of pipeline)
– DSD not applicable
– outstanding verifications to perform clean-up
– Safety risks: flare + HT/HP
 6-12 months after final completion
Initial clean-up Tune – continue
November /December 2002
Focus
 Initial clean-up
 Possible problems related to condensate blocking
Strategy
 Gradually opening of well
 Controlled by bottom hole pressure (Pdewpoint = 509 bar)
Measurements
 P/T sensors down hole and at wellhead
 Gas flow meter
 Online density meter on Tune separator
A-14 H – well trajectory
Geological cross-section along the drilled wellpath 31/8-A-14 H
BCU
Heather/Upper Tarbert
Lower Tarbert
TD
T2B1
T2B4
T2B2
T2B6
T2B5
T2B3
Well 30/8-A-14 H
 Horizontal section ~900 m
 Completed mid May 2002
 K/Cs-formate in reservoir section
30/8-A-12HT2
T2B5
T2B6
T2B4 T2B3
T2B2
T2B1
Heather/
Upper Tarbert
Lower Tarbert
A-12 T2H – well trajectory
 Horizontal section ~650 m
 Completed mid Nov 2001
Initially K-formeat in reservoir section
 Displaced to K/Cs-formate mid June 2002,
as upper completion was set
Tracers placed @
Antimonium - 4444 mMD RKB
Scandium - 4675 mMD RKB
Top reservoir @
4178 mMD RKB
TD @
4834 mMD RKB
A-11 AH – well trajectory
BCU
Top Res
Heather/
Upper Tarbert
“Lagoonal Event”
GOC
Lower Tarbert
OWC
 Horizontal section ~350 m
 Completed mid April 2002
K/Cs-formate in reservoir section
30/8-A-13H
T2B5
T2B6
T2B4
T2B2
T2B1
Upper Tarbert
Lower
Tarbert
T2B3
A-13 H – well trajectory
Tracers placed @
Silver - 4616 mMD RKB
Cobalt - 5031 mMD RKB
Top reservoir @
4241 mMD RKB
4829 mMD RKB
Lagoonal event
@ 5026 mMD
RKB
 Reservoir section ~900 m
 Completed mid Dec 2002
K-formate in reservoir section
Only well not displaced to K/Cs-formate
Overall performance Initial Clean-up
 Left for 6-12 months before clean-up
 Planned for 2-3 weeks
 10 - 24 hours per well
 Well performance
 Qgas 1.2 – 3.6 MSm3/d
 PI 35 – 200 kSm3/d/bar
 Well length sensitive
 No indication of formation damage
– Match to ideal well flow simulations (Prosper) - no skin
 Indications of successful clean-up
 Shut-in pressures
 Water samples during clean-up
– Formate and CaCO3 particles
 Registered high-density liquid in separator
 Tracer results
– A-12 T2H non detectable
– A-13 H tracer indicating flow from lower reservoir first detected 5 sd after
initial clean-up <-> doubled well productivity compared to initial flow data
 No processing problems Oseberg Field Center
SIWHP SIDHP SIWHP SIDHP
bara bara bara bara
A-11 AH 169 - 388 -
A-12 T2H 175 487 414 510
A-13 H 395 514 412 512
A-14 H 192 492 406 509
Before After
3350
3400
3450
3500
3550
3600
0 100 200 300 400 500 600 700 800 900 1000
Well length [m MD]
Depth[mTVDMSL]
A-11AH
A-12HT2
A-13H
A-14H
A-11 AH plugged back
Return of completion fluid
No quantitatively control of liquid flow during
start-up and first weeks of production
Spot ”water” samples of clean-up flow from
A-12 T2H and A-11 AH
 s.g. 0.8 - 1.33 pH 7.8 – 8.7
 CaCO3 particles
 Crushed Formation particles
Normal Production
 Stepwise increase in production to monitor well behaviour
(January 2003)
 Possible problems related to condensate blocking
 Production reached PDO defined plateau rate of 9 MSm3/d on
January 24th
 No negative effect on well productivity has been registered
 Ion analysis of produced water (January) - high content of
Potassium
 Pigging operation in March and June – minor/no formate
 Status June 2003
 All four wells producing
 Well productivity as expected
 Gas production 12.4 MSm3/d
 Condensate 23 000 bbls/d

Contenu connexe

Similaire à Production start-up in Tune gas condensate field, offshore Norway

Thebe River Safaris Room Addition 2014
Thebe River Safaris Room Addition 2014Thebe River Safaris Room Addition 2014
Thebe River Safaris Room Addition 2014
Grant Hepburn
 
Subsea well intervention: Learning from the past - planning for the future
Subsea well intervention: Learning from the past - planning for the futureSubsea well intervention: Learning from the past - planning for the future
Subsea well intervention: Learning from the past - planning for the future
Statoil
 
Hydrotest REPORT FOR 4'' 158m Line.
Hydrotest REPORT FOR 4'' 158m Line.Hydrotest REPORT FOR 4'' 158m Line.
Hydrotest REPORT FOR 4'' 158m Line.
Emeka Ngwobia
 
Integration From Multiple Disciplines in Horizontal Well Evaluations to Incre...
Integration From Multiple Disciplines in Horizontal Well Evaluations to Incre...Integration From Multiple Disciplines in Horizontal Well Evaluations to Incre...
Integration From Multiple Disciplines in Horizontal Well Evaluations to Incre...
Society of Petroleum Engineers - Argentine Section
 

Similaire à Production start-up in Tune gas condensate field, offshore Norway (20)

Mattias von Brömsse - Targetting safe aquifers
Mattias von Brömsse - Targetting safe aquifersMattias von Brömsse - Targetting safe aquifers
Mattias von Brömsse - Targetting safe aquifers
 
SUBSURFACE EVALUATION FULL SCALE EOR WATER FLOODING A - M FAULT ANTICLINE SHA...
SUBSURFACE EVALUATION FULL SCALE EOR WATER FLOODING A - M FAULT ANTICLINE SHA...SUBSURFACE EVALUATION FULL SCALE EOR WATER FLOODING A - M FAULT ANTICLINE SHA...
SUBSURFACE EVALUATION FULL SCALE EOR WATER FLOODING A - M FAULT ANTICLINE SHA...
 
Centennial Talk Hydrates
Centennial Talk HydratesCentennial Talk Hydrates
Centennial Talk Hydrates
 
Dev pumps
Dev pumpsDev pumps
Dev pumps
 
Quality Circle_ PRAYAAS_ 2023.pptx
Quality Circle_ PRAYAAS_ 2023.pptxQuality Circle_ PRAYAAS_ 2023.pptx
Quality Circle_ PRAYAAS_ 2023.pptx
 
Swimmey data sheet_en
Swimmey data sheet_enSwimmey data sheet_en
Swimmey data sheet_en
 
Seal-One Cantarell-418
Seal-One Cantarell-418Seal-One Cantarell-418
Seal-One Cantarell-418
 
filters
filtersfilters
filters
 
Nutrient Management in Everglades Agricultural Area (EAA) Canals
Nutrient Management in Everglades Agricultural Area (EAA) CanalsNutrient Management in Everglades Agricultural Area (EAA) Canals
Nutrient Management in Everglades Agricultural Area (EAA) Canals
 
Iapg jornadas shale neuquén vaca muerta a regional vision- 2013 neuquén
Iapg jornadas shale neuquén vaca muerta a regional vision- 2013 neuquénIapg jornadas shale neuquén vaca muerta a regional vision- 2013 neuquén
Iapg jornadas shale neuquén vaca muerta a regional vision- 2013 neuquén
 
Pool Filtration pdf document Aqua Middle East FZC
Pool Filtration pdf document Aqua Middle East FZCPool Filtration pdf document Aqua Middle East FZC
Pool Filtration pdf document Aqua Middle East FZC
 
Monitor drilling performance
Monitor drilling performanceMonitor drilling performance
Monitor drilling performance
 
Design water supply scheme
Design water supply schemeDesign water supply scheme
Design water supply scheme
 
Versocald - VERSOL steam boiler
Versocald - VERSOL steam boilerVersocald - VERSOL steam boiler
Versocald - VERSOL steam boiler
 
HDPE Pipes By Perfect Prime Piping & Agritech Private Limited, Rajasthan
HDPE Pipes By Perfect Prime Piping & Agritech Private Limited, RajasthanHDPE Pipes By Perfect Prime Piping & Agritech Private Limited, Rajasthan
HDPE Pipes By Perfect Prime Piping & Agritech Private Limited, Rajasthan
 
Thebe River Safaris Room Addition 2014
Thebe River Safaris Room Addition 2014Thebe River Safaris Room Addition 2014
Thebe River Safaris Room Addition 2014
 
Subsea well intervention: Learning from the past - planning for the future
Subsea well intervention: Learning from the past - planning for the futureSubsea well intervention: Learning from the past - planning for the future
Subsea well intervention: Learning from the past - planning for the future
 
Hydrotest REPORT FOR 4'' 158m Line.
Hydrotest REPORT FOR 4'' 158m Line.Hydrotest REPORT FOR 4'' 158m Line.
Hydrotest REPORT FOR 4'' 158m Line.
 
Integration From Multiple Disciplines in Horizontal Well Evaluations to Incre...
Integration From Multiple Disciplines in Horizontal Well Evaluations to Incre...Integration From Multiple Disciplines in Horizontal Well Evaluations to Incre...
Integration From Multiple Disciplines in Horizontal Well Evaluations to Incre...
 
CE Confr Presentation 08 Oct 2022.pptx
CE Confr Presentation 08 Oct 2022.pptxCE Confr Presentation 08 Oct 2022.pptx
CE Confr Presentation 08 Oct 2022.pptx
 

Plus de John Downs

SPE 145562 - Life Without Barite: Ten Years of Drilling Deep HPHT Gas Wells ...
SPE 145562 -  Life Without Barite: Ten Years of Drilling Deep HPHT Gas Wells ...SPE 145562 -  Life Without Barite: Ten Years of Drilling Deep HPHT Gas Wells ...
SPE 145562 - Life Without Barite: Ten Years of Drilling Deep HPHT Gas Wells ...
John Downs
 
SPE 165151 - The Long-term Production Performance of Deep HPHT Gas Condensat...
SPE 165151  - The Long-term Production Performance of Deep HPHT Gas Condensat...SPE 165151  - The Long-term Production Performance of Deep HPHT Gas Condensat...
SPE 165151 - The Long-term Production Performance of Deep HPHT Gas Condensat...
John Downs
 

Plus de John Downs (20)

BP Rhum field - Use of cesium formate kill pills during perforating
BP Rhum field - Use of cesium formate kill pills during perforatingBP Rhum field - Use of cesium formate kill pills during perforating
BP Rhum field - Use of cesium formate kill pills during perforating
 
SPE 24973 35 mm slides in Powerpoint .pptx
SPE 24973 35 mm slides in Powerpoint .pptxSPE 24973 35 mm slides in Powerpoint .pptx
SPE 24973 35 mm slides in Powerpoint .pptx
 
Formate fluids brochure from Forbrico Ltd 1996
Formate fluids brochure from Forbrico Ltd 1996Formate fluids brochure from Forbrico Ltd 1996
Formate fluids brochure from Forbrico Ltd 1996
 
SPE 26699 - TAME: A New Concept in Water-Based Drilling Fluids for Shales
SPE 26699 - TAME: A New Concept in Water-Based Drilling Fluids for Shales SPE 26699 - TAME: A New Concept in Water-Based Drilling Fluids for Shales
SPE 26699 - TAME: A New Concept in Water-Based Drilling Fluids for Shales
 
Single cell protein (SCP) from methane and methanol - publications from Shell...
Single cell protein (SCP) from methane and methanol - publications from Shell...Single cell protein (SCP) from methane and methanol - publications from Shell...
Single cell protein (SCP) from methane and methanol - publications from Shell...
 
A Walk Through Devon - Day 6 - Morchard Bishop to Five Crosses
A Walk Through Devon - Day 6 - Morchard Bishop to Five Crosses A Walk Through Devon - Day 6 - Morchard Bishop to Five Crosses
A Walk Through Devon - Day 6 - Morchard Bishop to Five Crosses
 
An introduction to formate brines - a technical presentation by John Downs, J...
An introduction to formate brines - a technical presentation by John Downs, J...An introduction to formate brines - a technical presentation by John Downs, J...
An introduction to formate brines - a technical presentation by John Downs, J...
 
A Walk through Devon - Day 5 - Bondleigh Bridge to Morchard Bishop
A Walk through Devon -  Day 5 - Bondleigh Bridge to Morchard Bishop A Walk through Devon -  Day 5 - Bondleigh Bridge to Morchard Bishop
A Walk through Devon - Day 5 - Bondleigh Bridge to Morchard Bishop
 
A Walk through Devon - Day 4 - Stockley Hamlet (Okehampton) to Bondleigh Bridge
A Walk through Devon -  Day 4 - Stockley Hamlet (Okehampton) to Bondleigh BridgeA Walk through Devon -  Day 4 - Stockley Hamlet (Okehampton) to Bondleigh Bridge
A Walk through Devon - Day 4 - Stockley Hamlet (Okehampton) to Bondleigh Bridge
 
Day 3 of a walk through Devon - Bridestowe to Okehampton
Day 3 of a walk through Devon - Bridestowe to Okehampton Day 3 of a walk through Devon - Bridestowe to Okehampton
Day 3 of a walk through Devon - Bridestowe to Okehampton
 
A walk through Devon - Day 2
A walk through Devon -  Day 2  A walk through Devon -  Day 2
A walk through Devon - Day 2
 
A walk through Devon - Day 1
A walk through Devon -  Day 1A walk through Devon -  Day 1
A walk through Devon - Day 1
 
SPE 199286 - Profiling the Production Performance of Five HPHT Gas Condensate...
SPE 199286 - Profiling the Production Performance of Five HPHT Gas Condensate...SPE 199286 - Profiling the Production Performance of Five HPHT Gas Condensate...
SPE 199286 - Profiling the Production Performance of Five HPHT Gas Condensate...
 
A walk through Cornwall from Lands End to Launceston - Day 11 of 11
A walk through Cornwall from Lands End to Launceston - Day 11 of 11 A walk through Cornwall from Lands End to Launceston - Day 11 of 11
A walk through Cornwall from Lands End to Launceston - Day 11 of 11
 
A Walk through Cornwall - Day 10
A Walk through Cornwall -  Day 10A Walk through Cornwall -  Day 10
A Walk through Cornwall - Day 10
 
A Walk through Cornwall - Day 9
A Walk through Cornwall -  Day 9 A Walk through Cornwall -  Day 9
A Walk through Cornwall - Day 9
 
SPE 145562 - Life Without Barite: Ten Years of Drilling Deep HPHT Gas Wells ...
SPE 145562 -  Life Without Barite: Ten Years of Drilling Deep HPHT Gas Wells ...SPE 145562 -  Life Without Barite: Ten Years of Drilling Deep HPHT Gas Wells ...
SPE 145562 - Life Without Barite: Ten Years of Drilling Deep HPHT Gas Wells ...
 
SPE 165151 - The Long-term Production Performance of Deep HPHT Gas Condensat...
SPE 165151  - The Long-term Production Performance of Deep HPHT Gas Condensat...SPE 165151  - The Long-term Production Performance of Deep HPHT Gas Condensat...
SPE 165151 - The Long-term Production Performance of Deep HPHT Gas Condensat...
 
A Ramble through Cornwall - Day 8 - Bodmin to St Neot
A Ramble through Cornwall - Day 8  - Bodmin to St Neot A Ramble through Cornwall - Day 8  - Bodmin to St Neot
A Ramble through Cornwall - Day 8 - Bodmin to St Neot
 
Formate matters-issue-10
Formate matters-issue-10Formate matters-issue-10
Formate matters-issue-10
 

Dernier

Structuring Teams and Portfolios for Success
Structuring Teams and Portfolios for SuccessStructuring Teams and Portfolios for Success
Structuring Teams and Portfolios for Success
UXDXConf
 

Dernier (20)

Buy Epson EcoTank L3210 Colour Printer Online.pptx
Buy Epson EcoTank L3210 Colour Printer Online.pptxBuy Epson EcoTank L3210 Colour Printer Online.pptx
Buy Epson EcoTank L3210 Colour Printer Online.pptx
 
Free and Effective: Making Flows Publicly Accessible, Yumi Ibrahimzade
Free and Effective: Making Flows Publicly Accessible, Yumi IbrahimzadeFree and Effective: Making Flows Publicly Accessible, Yumi Ibrahimzade
Free and Effective: Making Flows Publicly Accessible, Yumi Ibrahimzade
 
Syngulon - Selection technology May 2024.pdf
Syngulon - Selection technology May 2024.pdfSyngulon - Selection technology May 2024.pdf
Syngulon - Selection technology May 2024.pdf
 
Connecting the Dots in Product Design at KAYAK
Connecting the Dots in Product Design at KAYAKConnecting the Dots in Product Design at KAYAK
Connecting the Dots in Product Design at KAYAK
 
What's New in Teams Calling, Meetings and Devices April 2024
What's New in Teams Calling, Meetings and Devices April 2024What's New in Teams Calling, Meetings and Devices April 2024
What's New in Teams Calling, Meetings and Devices April 2024
 
10 Differences between Sales Cloud and CPQ, Blanka Doktorová
10 Differences between Sales Cloud and CPQ, Blanka Doktorová10 Differences between Sales Cloud and CPQ, Blanka Doktorová
10 Differences between Sales Cloud and CPQ, Blanka Doktorová
 
Linux Foundation Edge _ Overview of FDO Software Components _ Randy at Intel.pdf
Linux Foundation Edge _ Overview of FDO Software Components _ Randy at Intel.pdfLinux Foundation Edge _ Overview of FDO Software Components _ Randy at Intel.pdf
Linux Foundation Edge _ Overview of FDO Software Components _ Randy at Intel.pdf
 
ASRock Industrial FDO Solutions in Action for Industrial Edge AI _ Kenny at A...
ASRock Industrial FDO Solutions in Action for Industrial Edge AI _ Kenny at A...ASRock Industrial FDO Solutions in Action for Industrial Edge AI _ Kenny at A...
ASRock Industrial FDO Solutions in Action for Industrial Edge AI _ Kenny at A...
 
Behind the Scenes From the Manager's Chair: Decoding the Secrets of Successfu...
Behind the Scenes From the Manager's Chair: Decoding the Secrets of Successfu...Behind the Scenes From the Manager's Chair: Decoding the Secrets of Successfu...
Behind the Scenes From the Manager's Chair: Decoding the Secrets of Successfu...
 
Structuring Teams and Portfolios for Success
Structuring Teams and Portfolios for SuccessStructuring Teams and Portfolios for Success
Structuring Teams and Portfolios for Success
 
PLAI - Acceleration Program for Generative A.I. Startups
PLAI - Acceleration Program for Generative A.I. StartupsPLAI - Acceleration Program for Generative A.I. Startups
PLAI - Acceleration Program for Generative A.I. Startups
 
The Value of Certifying Products for FDO _ Paul at FIDO Alliance.pdf
The Value of Certifying Products for FDO _ Paul at FIDO Alliance.pdfThe Value of Certifying Products for FDO _ Paul at FIDO Alliance.pdf
The Value of Certifying Products for FDO _ Paul at FIDO Alliance.pdf
 
IoT Analytics Company Presentation May 2024
IoT Analytics Company Presentation May 2024IoT Analytics Company Presentation May 2024
IoT Analytics Company Presentation May 2024
 
UiPath Test Automation using UiPath Test Suite series, part 2
UiPath Test Automation using UiPath Test Suite series, part 2UiPath Test Automation using UiPath Test Suite series, part 2
UiPath Test Automation using UiPath Test Suite series, part 2
 
FDO for Camera, Sensor and Networking Device – Commercial Solutions from VinC...
FDO for Camera, Sensor and Networking Device – Commercial Solutions from VinC...FDO for Camera, Sensor and Networking Device – Commercial Solutions from VinC...
FDO for Camera, Sensor and Networking Device – Commercial Solutions from VinC...
 
Powerful Start- the Key to Project Success, Barbara Laskowska
Powerful Start- the Key to Project Success, Barbara LaskowskaPowerful Start- the Key to Project Success, Barbara Laskowska
Powerful Start- the Key to Project Success, Barbara Laskowska
 
Enterprise Knowledge Graphs - Data Summit 2024
Enterprise Knowledge Graphs - Data Summit 2024Enterprise Knowledge Graphs - Data Summit 2024
Enterprise Knowledge Graphs - Data Summit 2024
 
Custom Approval Process: A New Perspective, Pavel Hrbacek & Anindya Halder
Custom Approval Process: A New Perspective, Pavel Hrbacek & Anindya HalderCustom Approval Process: A New Perspective, Pavel Hrbacek & Anindya Halder
Custom Approval Process: A New Perspective, Pavel Hrbacek & Anindya Halder
 
The Metaverse: Are We There Yet?
The  Metaverse:    Are   We  There  Yet?The  Metaverse:    Are   We  There  Yet?
The Metaverse: Are We There Yet?
 
AI revolution and Salesforce, Jiří Karpíšek
AI revolution and Salesforce, Jiří KarpíšekAI revolution and Salesforce, Jiří Karpíšek
AI revolution and Salesforce, Jiří Karpíšek
 

Production start-up in Tune gas condensate field, offshore Norway

  • 1. Tune Case (NH) Experience from Clean-up and Production using formate based brines as drilling/completion fluids Drilling & Completion Fluid Seminar, Aberdeen 03.06.24 By Stine Bøhle Karlsen, Production Technology Tune
  • 2. Agenda – 03.06.24 Tune Field Information Initial clean-up / Normal Production Tune
  • 3. 3500 3500 3500 3500 3500 3500 35003500 3500 35003500 3500 3500 3500 3500 3500 3500 PPP 478000 479000 480000 481000 6701000 6702000 6703000 6704000 6705000 6706000 0 500 1000m 30/8-A-14H 30/8-A-12 H 30/8-A-13H/AH 30/8-3 30/8-1S 30/8-A-11 H 3750 3750 3750 3500 3500 3500 3500 35003500 3500 3500 3500 3500 3500 3500 PPP 475000 480000 485000 6695000 6700000 6705000 6710000 3850 - 3900 3800 - 3850 3750 - 3800 3700 - 3750 3650 - 3700 3600 - 3650 3550 - 3600 3500 - 3550 3450 - 3500 3400 - 3450 3350 - 3400 3300 - 3350 3250 - 3300 3200 - 3250 0 2000 4000m 30/8-A-12 H 30/8-A-13 H/AH 30/8-1S 30/8-A-11 H 30/8-A-14 H Tune Field  Horizontal gas producers  Pure gas depletion  Sand screen completion  Tarbert Formation  Gas/condensate  HP/HT – 525 bar / 131 degC  Reservoir thickness 100m - N/G 0.85  porosity ~16%, permeability 10-200 mD  12 m oil rim – non commercial 30/5-2
  • 4. Agenda – 03.06.24 Tune Key data Initial clean-up / Normal Production Tune
  • 5. Initial clean-up Tune PDO  To drilling rig (Deep Sea Delta)  2-3 weeks after final completion Actual  To Oseberg Field Centre (through 11 km of pipeline) – DSD not applicable – outstanding verifications to perform clean-up – Safety risks: flare + HT/HP  6-12 months after final completion
  • 6. Initial clean-up Tune – continue November /December 2002 Focus  Initial clean-up  Possible problems related to condensate blocking Strategy  Gradually opening of well  Controlled by bottom hole pressure (Pdewpoint = 509 bar) Measurements  P/T sensors down hole and at wellhead  Gas flow meter  Online density meter on Tune separator
  • 7. A-14 H – well trajectory Geological cross-section along the drilled wellpath 31/8-A-14 H BCU Heather/Upper Tarbert Lower Tarbert TD T2B1 T2B4 T2B2 T2B6 T2B5 T2B3 Well 30/8-A-14 H  Horizontal section ~900 m  Completed mid May 2002  K/Cs-formate in reservoir section
  • 8. 30/8-A-12HT2 T2B5 T2B6 T2B4 T2B3 T2B2 T2B1 Heather/ Upper Tarbert Lower Tarbert A-12 T2H – well trajectory  Horizontal section ~650 m  Completed mid Nov 2001 Initially K-formeat in reservoir section  Displaced to K/Cs-formate mid June 2002, as upper completion was set Tracers placed @ Antimonium - 4444 mMD RKB Scandium - 4675 mMD RKB Top reservoir @ 4178 mMD RKB TD @ 4834 mMD RKB
  • 9. A-11 AH – well trajectory BCU Top Res Heather/ Upper Tarbert “Lagoonal Event” GOC Lower Tarbert OWC  Horizontal section ~350 m  Completed mid April 2002 K/Cs-formate in reservoir section
  • 10. 30/8-A-13H T2B5 T2B6 T2B4 T2B2 T2B1 Upper Tarbert Lower Tarbert T2B3 A-13 H – well trajectory Tracers placed @ Silver - 4616 mMD RKB Cobalt - 5031 mMD RKB Top reservoir @ 4241 mMD RKB 4829 mMD RKB Lagoonal event @ 5026 mMD RKB  Reservoir section ~900 m  Completed mid Dec 2002 K-formate in reservoir section Only well not displaced to K/Cs-formate
  • 11. Overall performance Initial Clean-up  Left for 6-12 months before clean-up  Planned for 2-3 weeks  10 - 24 hours per well  Well performance  Qgas 1.2 – 3.6 MSm3/d  PI 35 – 200 kSm3/d/bar  Well length sensitive  No indication of formation damage – Match to ideal well flow simulations (Prosper) - no skin  Indications of successful clean-up  Shut-in pressures  Water samples during clean-up – Formate and CaCO3 particles  Registered high-density liquid in separator  Tracer results – A-12 T2H non detectable – A-13 H tracer indicating flow from lower reservoir first detected 5 sd after initial clean-up <-> doubled well productivity compared to initial flow data  No processing problems Oseberg Field Center SIWHP SIDHP SIWHP SIDHP bara bara bara bara A-11 AH 169 - 388 - A-12 T2H 175 487 414 510 A-13 H 395 514 412 512 A-14 H 192 492 406 509 Before After 3350 3400 3450 3500 3550 3600 0 100 200 300 400 500 600 700 800 900 1000 Well length [m MD] Depth[mTVDMSL] A-11AH A-12HT2 A-13H A-14H A-11 AH plugged back
  • 12. Return of completion fluid No quantitatively control of liquid flow during start-up and first weeks of production Spot ”water” samples of clean-up flow from A-12 T2H and A-11 AH  s.g. 0.8 - 1.33 pH 7.8 – 8.7  CaCO3 particles  Crushed Formation particles
  • 13. Normal Production  Stepwise increase in production to monitor well behaviour (January 2003)  Possible problems related to condensate blocking  Production reached PDO defined plateau rate of 9 MSm3/d on January 24th  No negative effect on well productivity has been registered  Ion analysis of produced water (January) - high content of Potassium  Pigging operation in March and June – minor/no formate  Status June 2003  All four wells producing  Well productivity as expected  Gas production 12.4 MSm3/d  Condensate 23 000 bbls/d