3. ABOUT TEAM
• NAME : SARYU SYNERGY
• DEPARTMENT : OPERATION & BMD
• FORMATION : MAY 2018
• DAY OF MEETING : WEDNESDAY
• TIME : 5:30-6:30 PM
• PERIOD : IN 15 DAYS
• NO. OF MEETINGS : 20
• % OF ATTENDANCE : 92%
• SOLVED PROBLEM : 09 ( TILL DATE)
SARYU SYNERGY
Better Together
4. ABOUT TEAM MEMBERS
COORDINATOR : SRAWAN KUMAR(OPN)
FACILITATOR : RAVI PAL SINGH(OPN)
TEAM LEADER : PANKAJ YADAV(BMD)
TEAM DY LEADER : ANIL KUMAR(BMD)
Team Members :DINESH KR YADAV(OPN)
RAMESH THAKUR(OPN)
SARYU SYNERGY
Better Together
SARYU SYNERGY
Better Together
6. STEP-1: IDENTIFICATION OF PROBLEMS
S NO. NAME OF PROBLEM CATEGORY
1. Atomizing Valve Oil Gun Gland Leakage A
2. Oil Gun Flange leakage A
3. Frequently damage of soot blower line flange gasket A
4. Soot blower line pressure gauge line leakage B
5. M.S. stop valve gland Leakage A
6. Safety Valve passing B
7. Oil gun choking problem A
8 Soot blower mechanical jamming. B
SARYU SYNERGY
Better Together
7. S NO. NAME OF PROBLEM CATEGORY
9. Phosphate dosing pump gudgeon pin circlip occasionally
damage.
A
10. Economizer lower most bend erosion problem. C
11. H2 leakage from gen-1 casing C
12. Turbine bearing vibration in unit#2 6h and 7h C
13. In unit #1 ID Fan A current hunting approximate 20A. B
14. Frequency of vertical shaft shearing of mill 1A C
15. Mill 4G continuous poor fineness B
16. Erosion of roller journal housing. A
STEP-1: IDENTIFICATION OF PROBLEMS SARYU SYNERGY
Better Together
8. S NO. NAME OF PROBLEM CATEGORY
17. Mill 2A less air flow. A
18. Hinge gate lever spring detachment. A
19. MRHS gate limit switch rod frequently broken. A
20. Mill 1A high vibration below 17A load. B
21. Feeder gear box lube oil leakage from oil seal. A
22. Lube oil leakage from shaft seal(DE) side in mill 2G C
23. View glass of return oil in mill 2 B not visible. A
24. CRH line LHS drain leakage in unit 1 near the condenser pass
A.
A
STEP-1: IDENTIFICATION OF PROBLEMS SARYU SYNERGY
Better Together
9. S NO. NAME OF PROBLEM CATEGORY
25. Steam leakage from Ext 7M valve flange in Unit#2. A
26. Frequent PF coal pipe leakages in all units. A
27. Steam leakage from steam ejector near the evacuation line . A
28. MRHS line mill G frequently chocking. B
29. U#2 MOT cooler I/L valve A-1 inoperative. B
30. RC feeder#2A I/L gate jamming and drum locking. A
31 U#1 TG Governing filter chocked but there was no alarm
persisted in Skoda system.
C
32. U#1 PA Fan #B jerky operation. C
STEP-1: IDENTIFICATION OF PROBLEMS
SARYU SYNERGY
Better Together
10. S NO. NAME OF PROBLEM CATEGORY
33. APH #2B duct punctured ,flue gas is on dangerous mode. A
34. U#1 barring gear motor cooling fan not available. C
35. U#1 Opacity#A getting out frequently. B
36. U#2 Oil splashing from Tg Bearing 7 lube oil return line . B
37. Station T/F incomer circuit breaker(6.6 KV) not closing in
remote.
C
38. BFP#2B discharge NRV passing. B
39. Mill G Seal air Line leakage A
40 Feeder & Centre pipe choking frequency of Mill G is more A
41 APH gearbox Failure C
STEP-1: IDENTIFICATION OF PROBLEMS
SARYU SYNERGY
Better Together
13. STEP-2: SELECTION OF PROBLEMS
Out of 41 identified problems 09 problems have been already solved
& implemented. From the remaining 32 problems we have selected 4
problems(one by each member).
S.No. Symbol Problem Selected By
2 P1 Oil Gun Flange leakage Anil Kumar
17 P2 Mill 2A less air flow. Dinesh Kumar Yadav
40 P3
Frequent choking of Mill G Feeder & Centre
pipe
Pankaj Yadav
33 P4
APH #2B duct punctured, flue gas is on
dangerous mode.
Ramesh Thakur
SARYU SYNERGY
Better Together
14. Points Assigned By Every Members To Each Problem (Scale 1 to 10)
Pankaj Yadav Anil Kumar
Criteria
Safety
Environ
ment
Urgency
Easy To
Work
Time
Saving
Total
Criteria
Safety
Environ
ment
Urgency
Easy To
Work
Time
Saving
Total
Problem Problem
P1 6 4 2 3 3 18 P1 2 3 6 2 6 19
P2 4 4 6 5 5 24 P2 1 3 8 9 3 24
P3 6 7 7 8 9 37 P3 6 8 8 9 4 35
P4 6 5 4 4 5 24 P4 2 4 3 7 5 21
Dinesh Kumar Yadav Ramesh Thakur
Criteria
Safety
Environ
ment
Urgency
Easy To
Work
Time
Saving
Total
Criteria
Safety
Environ
ment
Urgency
Easy To
Work
Time
Saving
Total
Problem Problem
P1 7 4 3 4 3 21 P1 3 3 6 4 3 19
P2 5 5 7 6 6 29 P2 5 2 4 3 1 15
P3 6 6 6 8 9 35 P3 3 8 6 5 7 29
P4 5 6 5 5 5 26 P4 6 7 2 6 1 22
STEP-2: SELECTION OF PROBLEMS
SARYU SYNERGY
Better Together
18. Q. C. Name Department Facilitator Members
SARYU SYNERGY O&M(OPERATION&BMD)
Mr. RAVI PAL SINGH
1. PANKAJ YADAV
(Leader)
Project Reason for selection 2. ANIL KUMAR
Prevent chocking of RC Feeder & Centre pipe of Mill G
due to wet coal
TO improve Mill G Availability 3. DINESH YADAV
Date of start
01.05.2018
Date of completion
30.10.2018
4. RAMESH THAKUR
S. N. Steps Weeks 1 2 3 4 5 6 7 8 9 10 11 12 Target Actual
1 Defining the problem 1
2 Analysis of the problem 2
3 Identification of causes 2
4 Root cause analysis 1
5
Data analysis of root
causes
1
6 Developing of solution 2
7
Foreseeing probable
resistances
1
8
Trial implementation and
check performance
1
9 Regular implementation 1
10 Follow up and review
Planning mile stone chart
(Project activity planning)
SARYU SYNERGY
Better Together
32. 0
2
4
6
8
10
12
14
1A 1B 1C 1D 1E 1F 1G 2A 2B 2C 2D 2E 2F 2G 3A 3B 3C 3D 3E 3F 3G 4A 4B 4C 4D 4E 4F 4G
Bar Chart-Frequency of choking between 01.05.2017 to
30.10.2017
RC Feeder#G
has more
choking
STEP-4: ANALYZE THE PROBLEM
SARYU SYNERGY
Better Together
38. STEP-5: FIND OUT CAUSES
SARYU SYNERGY
Better Together
12 probable causes have been found through brain storming method and the list has been
classified into 04 categories by stratification method
MAN
Laziness in cleaning
Improper coal cleaning
Wrong pin closing method
MACHINE
Complicated system
Extra pin type gate
Extra feeder outlet gate
METHOD
• More time taking
• Wet Coal sticking on feeder
body
• Wet coal sticking on center
pipe
MATERIAL
• Penetration of gate plate is
difficult
• Coal accumulation
• MS PIN IN WET COAL
CAUSE
41. STEP-6: FIND OUT ROOT CAUSE
SARYU SYNERGY
Better Together
MAIN CAUSE SUB CAUSE VALIDITY RANK OUT OF 10
MAN
UNTRAINED MANPOWER USED NO 0
LACK OF MANPOWER NO 0
FATIGUE YES 1
MACHINE
WRONG POSITION OF MANHOLE YES 1
GATE PLATE RAKE THICKNESS MORE YES 10
HEAVY COAL LOAD YES 1
METHOD
DIFFICULT PIN & PLATE CLOSING YES 1
IMPROPER FEEDER BODY CLEANING YES 1
IMPROPER CENTER PIPE CLEANING YES 1
MATERIAL
JAMMING OF MS PIN YES 10
WET COAL YES 3
BLIND HOLE RAKE YES 2
VALIDATION METHOD
46. STEP-8: DEVELOPMENT OF SOLUTION
SN. SOLUTION ACCEPT/REJECT REASON
1 USE SERVICE AIR IN CENTER PIPE BETWEEN
BUNKER AND FEEDER
REJECT •REQUIRE NEW COMPRESSOR
•HAVE HIGH COST
2 BY CHANGE WITH NEW FEEDER REJECT •HIGH COST
•SAME PROBLEM
3 POKING IN CENTER PIPE MAN HOLE WITH
USING A LONG BAR
REJECT •MORE MANPOWER FOR POKING
•HAZARDOUS
4 CHANGE THE DESIGN OF FEEDER REJECT •HIGH COST OF DEVELOPMENT
5 HAMMERING ON CENTER PIPE REJECT •REQUIRE EXTRA MANPOWER
•COSTLY
6 PROVIDE A POKING HOLE IN CENTER PIPE REJECT •ONLY PARTIAL CHOKING CLEAR
7 USE SKILLED LABOUR FOR HAMEERING OF
FEEDER
REJECT •HIGH COST
8 REPALCE FEEDER INLET GATE FROM PIN TYPE
TO PLATE TYPE PROVIDED BY OEM
REJECT •PROVEN IN OTHER FEEDERS
•COSTLY AND TIME TAKING
9 REPALCE FEEDER INLET GATE FROM PIN TYPE
TO PLATE TYPE FABRICATED INHOUSE.
ACCEPT •PROVEN IN OTHER FEEDERS
•CHEAPEST AND QUICKEST
SARYU SYNERGY
Better Together
49. STEP-9: FORESEEING PROBABLE RESISTANCE
SARYU SYNERGY
Better Together
By Brain storming our team have identified the following probable constraints and
found the ways to overcome them..
Sl No RESISTANCE ELIMINATION
1 BUNKER EMPTY BUNKER EMPTY ONLY DURING
OVERHAULING
2 MATERIAL AND FABRICATION MATERIAL ARRANGED FROM BMD STORE
COMPONENT PRE FABRICATED IN CENTRAL
WORKSHOP
3 PERMISSION FOR
IMPLEMENTATION OF
SOLUTION
DEPARTMENTAL NOTE FOR APPROVAL
4 15 DAYS FOR
IMPLEMENTATION OF
SOLUTION
SOLUTION IMPLEMENTED DURING
OVERHAULING
55. 0
2
4
6
8
10
12
14
16
1A 1B 1C 1D 1E 1F 1G 2A 2B 2C 2D 2E 2F 2G 3A 3B 3C 3D 3E 3F 3G 4A 4B 4C 4D 4E 4F 4G
Frequency of choking between 01.05.2018 to 30.10.2018
Frequency of choking between 01.05.2017 to 30.10.2017
STEP-10: TRIAL IMPLEMENTATION AND
CHECK PERFORMANCE Unit#3,4 gates
replaced and
frequency of
choking reducedUnit#1,2
frequency of
choking is nearly
same
SARYU SYNERGY
Better Together
59. STEP-12: FOLLOW-UP AND REVIEW
SARYU SYNERGY
Better Together
Comparative mile stone chart for checking performance
S. N. Steps Weeks 1 2 3 4 5 6 7 8 9 10 11 12 Target Actual
1 Defining the problem 1 1
2 Analysis of the problem 2 2
3 Identification of causes 2 2
4 Root cause analysis 1 1
5 Data analysis of root 1 1
6 Developing of solution 2 2
7 Foreseeing probable 1 1
8 Trial implementation and 1 2
9 Regular implementation 1 1
10
Follow up and review
Q. C. Name Department Facilitator Members
SARYU SYNERGY O&M(OPERATION&BMD)
Mr. RAVI PAL SINGH
1. PANKAJ YADAV
(Leader)
Project Reason for selection 2. ANIL KUMAR
Prevent chocking of RC Feeder & Centre pipe of Mill G
due to wet coal
TO improve Mill G Availability 3. DINESH YADAV
Date of start
01.05.2018
Date of completion
30.10.2018
4. RAMESH THAKUR
61. COST OF FEEDER GATE
COST OF BEARING- CAM FOLLOWER -
RATE OF BEARING-CAM FOLLOWER -700RUPEES/ PIECE
NO OF BEARING (CAM FOLLOWER) – 10 PIECE
TOTAL COST OF( BEARING- CAM FOLLOWER ) - 7000 RUPEES
COST OF 6306 BEARING -
RATE OF 6306 - 400 RUPEES/ PIECE
NO OF 6306 BEARING – 02 PIECE
TOTAL COST OF 6306 BEARING - 800 RUPEES
TOTAL COST OF MS SPUR GEAR (200MM) FROM WORKSHOP -4000 RUPEES
TOTAL FABRICATION COST FROM WORKSHOP – 20,000 RUPEES
TOTAL IMPLIMENTATION COST = TOTAL COST OF 10 MM SHEETS +TOTAL COST
OF 8 MM SHEETS +TOTAL COST OF 8 MM LINER ( SS) + TOTAL COST OF
(BEARING- CAM FOLLOWER ) + COST OF 6306 BEARING + TOTAL COST OF MS
SPUR GEAR (200MM) FROM WORKSHOP+ TOTAL FABRICATION COST FROM
WORKSHOP = (32,633.70 + 902.93 +20,440 + 7,000 +800 +4,000+20,000) RUPEES
= 85776.33 RUPEES
63. ADVANTAGES
STEP-12: FOLLOW-UP AND REVIEW
SARYU SYNERGY
Better Together
TANGIBLE ADVANTAGES INTANGIBLE ADVANTAGES
• Exposure of cross functional area.
• Exposure to QC tools and techniques.
• Motivation and better team spirit.
• Feeling of achievement among team
members.
• Reduce operational stress.
• Rs 95,70,000.00 saved in LDO per
annum.
• Rs 12,54,000.00 saved by preventing
even one tripping of Unit on flame loss.
• Availability of bottom Mill#G and RC
Feeder#G is improved.
• Stability of Unit by availability of Mill#G.